After a failed attempt to do some mapping which resulted in most of the pictures NOT being taken, and the ones that were taken being very blurry, I went through my 3DR EAI S100 Lua script and found a lot of the settings had been changed. It has proba
I have been using a separate battery in the past - but now I want to trim down on things I need to take with me when I fly (and prepare/charge etc) so I want to power the gimbal from the flight battery.
I had a very heaving landing in RTL today - the descent was much faster than usual, it literally almost dropped out the sky. I suspect my battery failsafe is set too low and the voltage tapered off quickly as the battery ran out and that was
I ordered the 11 x 4.5 MR/MRP props from APC, and they arrived without the little adapter rings (apparently you have to purchase those separately... Doh!).
I tried to fit them to my stock 3dr quad kit (with the 880kV motors) but the internal diameter
I had a scary experience today using loiter. I had the quad about 3 metres off the ground and switched from Loiter to Stabilize and the mid throttle position did not provide enough thrust so the craft came to ground too fast for me to adjust. Fortuna
I have a 4000mAh 3c Turnigy Nano-tech Battery, and I am confused about what to put in the "Battery Failsafe (mAh)" setting. There is nothing mentioned in online wiki about the "mAh" setting - only the Voltage.
Hello everyone,I have a problem with my 3dr DIY Quad (running latest release) with mission planner 2 (Mac) setup with Taranis + X8R.Motor #2 does not want to play ball.With Pixhawk armed, prop does not spin like the others until a gentle throttle app